Thread: 3S-GTE USDM Turbo Engine MK2 NA > Turbo Write-Up
View Single Post
Old 09-10-2009, 04:56 PM   #125 (permalink)
DrWonderEyes
MR2 + 400hp = Fun
 
DrWonderEyes's Avatar
 
Join Date: May 2006
Location: Florida
Posts: 780
Thanks: 3
Thanked 16 Times in 16 Posts





Send a message via ICQ to DrWonderEyes Send a message via AIM to DrWonderEyes Send a message via MSN to DrWonderEyes Send a message via Yahoo to DrWonderEyes
talk about a nightmare lol
the swap i did. the motor had a bad freeze plug behind the altenator bracket. changed that. the ECU had a bad capacitor (the one that the IGF and IGT signals pass through) and cause the car to go into limp mode like as if u hit fuel cut from over boosting thusly cutting ignitor voltage.

anyway fixed all taht stuff. if anyone has GEN3 issues with it not running right. i'll show u what capacitor goes bad on the motherboard of the ECU.

this write up did help me a little. so i appreciate it
DrWonderEyes is offline   Reply With Quote
 
Page generated in 0.13071 seconds with 16 queries