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| Forced Induction Turbocharged, Supercharged, Twin-Charged, or Leaf Blower Charged - It's all in here. |
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#1 (permalink) |
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some skills
Join Date: Oct 2007
Location: New Zealand
Posts: 93
Thanks: 11
Thanked 5 Times in 4 Posts
iTrader Rating: (0/0% ) |
Boost issues... please help !
I have an aw11 4agze with oversize crank pulley which usually hits 11.5psi on my boost guage WOT in 5th gear. However after a recent track day (where it performed awesome ALL day) it started only boosting half, EXACTLY half?!
so now, if i floor it, it shoots up to about 6-7psi on the guage then after one second levels off to about 5 psi so i know your thinking intercooler pipe leak right ? i took off the intercooler and the pipes from the SC to the throttle body all look sweet, so what else could it be ??? cheers guys |
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#2 (permalink) |
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Get your -_- face on
Join Date: Aug 2008
Location: New Zealand
Posts: 2,156
Thanks: 17
Thanked 127 Times in 111 Posts
My Google Map iTrader Rating: (0/0% ) |
Belt is not loose and slipping? There is not a huge amount of things I can think of to cause that. Either that or the supercharger clutch could be starting to slip which I don't know how to check for other than pulling it apart.
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| The Following User Says Thank You to 328FTW For This Useful Post: | Angus (12-20-2008) |
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#3 (permalink) |
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Cage Fighter
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clogged intake (air filter)
THE USUAL SUSPECTS: leak in IC, or intake piping to and from SC to head. Including intake manifold. Loose, missing, or unplugged vacuum lines. I don't know is the safety experts would approve, but I spray brake cleaner on, and around suspected leak areas. Do this in moderation, don't allow puddles of the spray to form. Do it while idling the engine. If the engine idle "wobbles" or reacts to the presense of the brake cleaner . . . there is your leak. If you can't find an intake restriction, or leak . . . pull the SC out. Disassemble it, and see if the rotors are melted, warped, or have too much clearance from the case's interior. Good Luck Bloke! |
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| The Following User Says Thank You to Jackstand Queen For This Useful Post: | Angus (12-20-2008) |
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#4 (permalink) | |
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some skills
Join Date: Oct 2007
Location: New Zealand
Posts: 93
Thanks: 11
Thanked 5 Times in 4 Posts
iTrader Rating: (0/0% ) |
Quote:
cheers for the thought though my mechanic cant figure it out, so like many other times, i come to you guys for help ![]() |
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#5 (permalink) | |
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some skills
Join Date: Oct 2007
Location: New Zealand
Posts: 93
Thanks: 11
Thanked 5 Times in 4 Posts
iTrader Rating: (0/0% ) |
Quote:
ill look at the air cleaner, probably needs a clean, and re-oil by now I really appreciate the thoughts guys |
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#6 (permalink) |
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three mk1's
Join Date: Feb 2006
Location: NC
Posts: 453
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I know you said you checked the IC and SC pipes, but did you check the rubber coupling down low coming off the S/C and going to the charge pipe or whatever that thing is called? Of course that one is the hard one to reach, but when I had the same type deal happen I found a 1 inch or so long gash through my lower pipe. I replaced all 4 rubber sections with hard rubber radiator hose of the same size and boost increased 1.5 lbs over what I had been boosting and throttle response improved slightly under boost
. Cheapest performance mod bang-for-your-buck wise for the S/C car I've ever heard of. It sounds so simple, and is total common sense, but really seems to work great!! If you've got those off, go ahead and try the radiator hose straight pipe instead of the ones with the bulge... the bulge kills aero and creates a slight delay as each pipe bulges under boost. I think it cost me maybe 8 bucks for the 4 sections of pipe from NAPA and I have run them for over a year with no problems... have removed and checked a couple sections to verify that they are holding up well, and they are so far. |
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| The Following User Says Thank You to curvesrgood For This Useful Post: | Angus (12-21-2008) |
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#7 (permalink) |
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some skills
Join Date: Oct 2007
Location: New Zealand
Posts: 93
Thanks: 11
Thanked 5 Times in 4 Posts
iTrader Rating: (0/0% ) |
Thanks heaps guys
finally got around to looking at it again, and i checked the super to intercooler pipe from underneath the car and it was all good, so started checking the vacuum hoses and the one going onto the ABV was not on tight, so i pushed that on fully and when for a drive and its all good again, full boost ! Had to believe something that minor could cut the boost in half. So she is back in business, and im a very happy man again Happy holidays ! |
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